2002/03/31
Bought car from Preston Clark of Bishop, CA.
Car is running with some problems, particularly gauges,
instruments, timing and fuel mixture. Car is mostly original,
but has TR4a carbs (the HS6 instead of H6 SU carbs), radiator
is missing crankstart hole, has
elec fan.
2002/04
Odometer reading: 8400mi (probably not even the original odometer,
so I can't even guess that it's 108k or 208k miles..)
2002/04
Had to grind down front bonnet - it was too long on one side
and squeaking.
Replaced brake light pressure switch
Rebuilt carbs.
Replaced ignition with Pertronix electronic ignition,
monkeyed with timing (had to un-sieze distributor pedestal)
Minor cosmetics, attached vent panel, pedal covers, etc..
2002/05
Replaced steering column electricals (horn wasn't working).
Consequently, turn signals and headlights both went out as
well, fixed some fusing problems and rewired, now lights,
signals and horn all work.
Replaced oil filter with screw-on adaptor and changed oil.
(replacements are Fram #PH3600 and K&N #HP-2009: 1971 Pinto, amongst others)
2002/06
Valve job, replaced valve seal.
Upholstered some of the loose rear body capping/trim
2002/08
Brake fluid leak. Replaced master cylinder and unfortunately broke
Bundy tube, replaced tubes and tightened up reservoir leaks.
Bled all the nasty 1957 brake fluid out of the system.
2002/09/27
Replaced oil pan gasket. Messy, difficult job.
2002/10/10
Got starter rebuilt at RiteWay Electric. Don't go there, they
are a miserable company to work with and they did a miserable job.
2002/10/24
Lengthened/replaced too short power cables behind dash
Bled the clutch (didn't fix problem in the end)
Disassembled/repaired flakey headlight dimmer switch.
2002/11/04
Replaced glove compartment with wood shelf (for mounting stereo)
Flipped over choke cable so it locks again
Replaced heater core motor with spare and hooked up core
Rebuilt heater rheostat switch - heater now works!
2002/11/12
Catastrophe on 11/8! Gas tank springs a leak and spills 2/3 tank
over garage floor. I pull the gas tank and have it repaired.
2002/11/17
Replace clutch master cylinder.
2002/11/30?
Replace left-rear leaf spring (cracked) by Carlos Automotive
2002/12/04
Replace first muffler and redirect pipe by Discount Muffler
2002/12/04
Pull starter and bring to RiteWay for more work - they claim it's
the flywheel that's the problem. Ugh.
Finish 11/12 gas tank repair by replacing filler neck hose.
2003/01/08?
Start building my custom backseat/stereo compartment
2003/01/23
Antifreeze leak! Traced to heater valve hose - cut and tightened.
Replaced hood hinge gaskets and tightened - no more squeaks!
2003/01/27
Fan switch broke (on 1/23), finally tracked down replacement.
2003/03/21
Finished basic frame for backseat
2003/03/24
Got wiper motor fixed
Took in backseat top for upholstery and passenger seat
for re-upholstery
Got a flat tire on the way home. Grrr.. Replaced with spare
which also went flat. Grrr... Fixed flat, and then something
was grinding when the wheel rotated - turns out the wheel is
now hitting the calipers. :(
2003/03/25
Disassembled front hubs and pulled out wheel bearings.
2003/03/26
New bearings came in - doesn't solve problem.
Turns out the caliper mounting plate on the left is wrong, and
it didn't have enough clearance, and finally it started to hit.
2003/03/29
Replaced caliper mounting plate, problem fixed!
Picked up and installed seats from upholstery shop.
2003/03/30
New tires
2003/04/01
Created wooden trunk cover for stereo project
Painted cover and backseat.
2003/05/07
Repaired wiring in dash and to lights. Added a homemade wiring
harness extension so I can pull dash out while still connected.
2003/08/23
3 of 4 driveshaft bolts came out! Crikey! And this happened
just as I was coming up to speed on the freeway - if it had
happened 30 seconds later I would've been in big trouble.
Managed to get it to a shop that had replacement bolts.
2003/09/02
I come back from vacation and the TR3A is blowing smoke and
has no power. Head gasket?
2003/09/11
I bite the bullet and pull the head, my first real engine work.
Turns out the head gasket is practically fused to the block and
won't give. After some robots help me,
I get the head off and sure enough discover a blown gasket.
2003/09/16
I replace the head gasket, and the car runs. But then everything
else falls apart. The generator stops generating, one of the
flasher bulbs burns, one of the manifold bolts breaks, another one gets stripped,
and once again the driveshaft bolts fall out. Looks like the shop
didn't do such a stellar job. When replacing the driveshaft bolts
I notice that the two nuts for the rear frame bolts for the
transmission have fallen out at some point as well, one of the nuts
is still sitting on the ledge below it, saved by the oily gunk
deposits there. Looks like I need to spend some time under my car
checking all the nuts.
2003/09/17
I replace/fix all the bolts and the flasher and replace a radiator
hose clamp that got stripped.
2003/09
Car is running poorly, then finally dies. Seems like it's misfiring mightily.
2003/10/02?
Turns out both the rotor and the distributor cap went bad. Car
is running again, but poorly and it's fouling plugs.
2003/10/09
Carlos figures out that somehow the distributor gear has jumped a tooth,
which explains how the timing is so far off. This fixes the running
problems, at least for a while, but then it starts misfiring occasionally
again. My car is cursed! I still haven't rebuilt the generator
(I just hook it up to a charger), so I'm speculating that it's not
getting enough power to fully spark. Maybe it's time to finally
do that alternator conversion..
2003/12/03
Converted to negative ground in preparation for an
alternator conversion.
It was easy, basically:
- Disconnect battery, turn around, connect negative -> ground
- Flip coil leads: (-) to distributor, (+) to ignition switch.
- Disconnect generator, briefly touch field (F) terminal on generator
several times with wire to (+) on battery to spark (this
repolarises the field windings)
- Convert back to condensor/points because my pertronix electronic
ignition unit was positive ground. Anyone want to buy it?
- Connect battery positive.
I'll worry about flipping the ammeter nodes later.
2003/12/05
I pull out the manifolds again and look at the broken manifold bolt.
Sure enough it broke off flush with the block. I'll need to deal
with that later. I get an AC Delco alternator and try to figure
out how to do the alternator conversion, I'll be putting photos
up as soon as I figure it out.
2003/12/13
The bolt that got stripped was because the manifold holes were
too close(?). I grind out one of the holes so it can fit on the
new stud that I've installed to replace the bolt.
I send in the exhaust manifold to Jet-Hot to get it recoated.
You can see the results yourself.
2004/02/02
Flushed the radiator.
Fixed the wiper again. This time I custom made a spring to replace
the old brush spring. It still draws too much current though, and
sometimes blows the fuse.
2004/02/21
Fixed the door handles
2004/02/24
Did some research on the alternator conversion
- I might finally have a solution.
Built the electric lock for the
glove compartment - need to find a way to mount it and the strike plate.
Cut a back panel for the glove compartment. Need to make sure it's
water-tight and probably going to take it out one last time to paint it.
2004/03/18
Odometer reading: 16700mi
2004/04/06
The head gasket blew again. The compression is even higher (210-220) and
I'm now finding out that it should be around 175. Turns out the original
head thickness was 3.325 - 3.330 and it should never be milled below 3.170,
otherwise the combustion chamber gets too small and compression gets
too high, and poof goes the gasket).
2004/04/07
Sure enough, I pull the head and the gasket looks like it's been forced
open. This explains why the head gasket nuts were torqued down so far,
looks like the previous seller had seen this problem and was using
nut pressure to avoid blowing gaskets. I take it to a machine shop
and find that I'm running about 3.180 (and there's a small crack
in the center across the water channel to boot). Fortunately it's not
warped. I order a shim (694-505 - not in their online catalog) from
Moss and have the machine shop start the repair. Moss also recommends
using coppercoat to improve the seal, so I order some of that.
2004/04/07
It's a busy day. Perhaps feeling guilty for the dead state of my car,
I crank away at small jobs:
Finish bolting in the speakers and staple down the speaker covers.
Put in an electric antenna.
Finished the glove compartment electric lock and strike (just needs a
switch and a spring).
..tomorrow it's going to be the alarm system and back seat lock.
2004/04/11
I finally found an alternator solution!
2004/04/13
Built backseat lock (similar to glove compartment) and ripped out interior
to start running wire for alarm and stereo.
2004/04/18
Odometer reading: 16900mi
Put the engine back together.
Unfortunately the compression is even higher regardless of the shim, so
I need to find another head.
2004/04/28
Engine still misfiring. I hooked it up to a scope and the spark lines
were all squiggly. That's bad. When I pulled the spark plug wire and
sparked to the engine block, it was clean, so something is happening
inside the cylinder. Perhaps the incredibly high compression is
screwing up the spark? The coil was giving out about 35kV, which
I think I read as being fairly normal for the stock coil. Anyone?
I also finished hooking up a door switch (because the damn alarm wants
to know when the door is opened or closed or else it won't work. Bah.)
And finally, the wiring harness is done for the alarm system!
2004/04/29
Finished the wiring for the amp and speakers.
I have sound!
I found another head (Power British had some) and took it to the machine
shop to get it checked out and cleaned up.
2004/05/04
Welded new hold in for new door check strap for driver door.
Turn signal fuse (A2) keeps blowing, put in temp flasher to test.
Installed Pertronix negative ground kit. Anyone want to buy the
positive ground pertronix electronic ignitor? I noticed the distributor
plate wasn't attached very well to the body anymore - might be stripped,
need to look into getting another distributor body to test.
2004/05/06?
Pertronix ignitor dies! I replace with points/condensor which are
fortunately still working.
2004/05/19
Took off the head (hopefully for the last time) to prep for the new head.
Record removal time of under 1.5 hours.
2004/05/??
Replaced head. Fixed some connections in the distributor and reset points.
Car runs without misfiring!
2004/06/04
Fixed signals - problem was bad connector from steering wheel.
Pulled off valves and replaced a few threaded and junky rocker arm
adjustment screws, and retightened the head. Flushed the radiator.
Wiper motor blown. Annoying. I have a replacement to install.
2004/07/20
The car is getting a full body restoration and a paint job.
2004/09/20
Happy 47th Birthday!
2004/09/25
Odometer reading: 18244mi
One more head gasket job, this time demonstrating a faster
technique
Finished alarm install (but alarm has some bugs..)
Fixed shaky brake light connection from paint job reassembly.
2004/12/17
The suspension siezed up back in November. I tore it apart and figured
out that the trunnion was bad, so I ordered another. When it showed up
I realized my suspension was missing some parts, so I placed another order.
Then I mistakenly damaged the new trunnion, so I ordered another.
Then when my garage was rearranged, some parts were lost, so I placed another
order. Then I needed some more parts, so..
Ugh. It was a nightmare. Finally I got the trunnion replaced and
put my suspension back together and it works!
It was quite a learning process about how to take
apart the front suspension
2005/03/??
Odometer reading: 18814mi
Transmission finally blew out. Damn. This car isn't happy these days.
The first and reverse gear are shot, but 2-4 still work.
2005/04/25
Much as I'd love to learn about pulling a transmission, I simply don't
have the time, so I finally give in and let my mechanic Carlos pull it out.
Turns out 1st is chewed up and the reverse/countershaft gear is in bad
shape, but the rest of the gears look not so bad.
2005/06/02
Picked up my car today! Transmission is rebuilt. Found a NOS first gear
and a decent used countershaft, and bought the requisite bearings and
synchros for a rebuild.
While the car was in the shop I finally pulled the carbs and took them
to a machine shop to bore out the butterfly valve shafts for oversize
shafts, finally the idle is stable and the car isn't dieseling anymore.
The mix is off, so I need to adjust the carbs, maybe next week.
2005/06/06
Got in the replacement electric ignition (pertronix ignitor).
The battery is low (still having charging problems?) so I'm charging it.
2006/02/05
The right turn signal hadn't been working, and I finally tracked it
down, turns out the connector in the horn/turn switch had broken off
again, so I needed to pull that apart and repair it - those switches
are a nightmare. Maybe next time I'll take photos.
Haven't figured out charge problems, but I cleaned up an alternator connection.
The transmission is still having trouble with 3rd gear and I keep losing
clutch fluid. Furthermore, I rather surprisingly had all of the brake
fluid disappear one day - I think perhaps the seals are falling apart
(though I don't know why the brakes would be emptied). Last of all,
someone hit my car recently and scratched the hell out of the rear left panel.
*sigh*. It's a rough time to be my car right now, evidently.
2006/03/09
I get the rear panel refinished.
2006/08/??
I replace the battery, this seems to ameliorate the charging problems,
don't know if it solved them.
2006/09/23
I keep losing brake fluid. The brakes get worse, and I finally pull
the rears apart. The cylinders are gushing fluid, and need to be
repaired and the shoes replaced. At some point the wrong fluid was
introduced to the system and ate all the old seals, probably when the
transmission was rebuilt. I'll pull the front brakes and clutch slave
next to see if they're shot as well.
2006/10/19
Finally got new drums. Repainted hubs & inside of right wheel where
the brake fluid had removed most of the paint. Rebuilt brake cylinders,
reassembled and bled all brake lines. Brakes are happy, but 3rd gear
is still troubled.
2007/02/24
A few things. Left door handle has broken loose and caused some
door damage. The shifter knob medallion popped off. The body work
under the drivers door (which was cracked) has gotten worse (a few
weeks ago) and has been squeaking. The car is also running poorly,
need to check tune and spark plugs (Champion L87Y/NGK BP6HS). (Champion #327
is evidently "Copper Plus #RL87YC"). Also, one of the tires keeps
going flat. Poor car.
2007/04/25
Replaced spark plugs, big improvement. Also took off door handle,
though I need to bring the door in for repair now, and I need
to get some washer/nuts for the new door handle. Shifter medallion
was fixed a few weeks back.
2007/10/22
Sadness. I have an accident
2008/01/04
The muffler's finally dead (after enough times of the exhaust scraping my
driveway). I take it to Chris' Muffler, but he replaces it with a resonator,
so I'm going to take it back.
2008/01/10
I finally tune my carbs which were way too rich.
I also order new (washable) air filters which look pretty fine, actually,
and a stainless steel exhaust system which also turns out nice
(after a few attempts at installing).
2008/02/04
My car stops charging, again. Much to my surprise, the engine pulley
is broken. Fortunately this doesn't require pulling the engine. I also
take my car back to Chris' Muffler to get the stainless exhaust installed.
2008/02/12
Odometer reading: 23407mi
I get the pulley replaced and realize that I can do a better job lining
up the belt by putting the spacers behind the alternator and pushing
it forward more than (I remember) the instructions claim. Car is charging
fine and the belt tension seems to hold.
2008/03?
Transmission dies again. *grrr*
That's only 3 years. Third gear never shifted very smoothly, but surprisingly
it was the 1st/Reverse gear that died again, rather surprisingly and without
any warning.
2008/04/24
I pull the transmission. The bearings are in bad shape and the transmission
seems to be leaking some oil into the bell housing. The release bearing
is completely shot. I also notice that the gear change stay bracket has
disappeared sometime in the last 50 years, as well as the clutch housing
cover, I'm lucky no rocks happened up there to chew-up the clutch or flywheel.
I end up putting in a
Toyota Transmission with the HVDA conversion kit.
There's some play in the front U-Joint, so I replace those as well.
The rear main seal has some oil leaking, but evidently that's
common and unavoidable (unless I want to pull the crankshaft and convert
to a rubber seal. Not today.)
While it's apart, I clean off the seat panels and paint them with a rust
protect primer.
The conversion is functional, but I still need to put the panels and
carpet back together (after getting back from vacation. :)